On the EGR line, I cut the pipe that went from the engine block to the intake manifold. I then plugged the portion that went into the manifold. The other end appeared to have a pump mechanism on it. I put an angled fitting onto it and routed it toward the bottom the engine compartment. I know the manual stated to leave it alone but when I opened up the throttle body, it was absolutely filthy with a brownish, tarry substance covering everything engine side of the butterfly. I just couldn't see letting this filth continue to be drawn inside the engine. A side note, I have a 2007 Chev duramax pickup and they strongly encourage owners to block the EGR system. I didn't until at 75,000 miles my turbo froze up from the same tar filth. $2,000 later I'm back running but with an EGR blocker plate. That was my reasoning for messing with the EGR on the van.
The PCV valve, the manual addresses several spots that I found. One said to simply put JB weld into the PCV valve, effectively plugging it and then put the hoses back in place. The other talked about rerouting the system. I understood, leaving the valve functioning but not going into the intake manifold, instead, reroute it so it enters the airstream between the air filter and the TB. I split the difference. I took the hose off the manifold fitting and plugged it securely but then installed an elbow fitting and just vented the PCV into the open air.
There is 180,000 on the 05 Town and country. I put both new oxygen sensors in it, opened the plug gap ,010 to .060 (.050 recommended), checked all the vacuum lines coming out of the manifold and they all held 20" vacuum. After warming up the engine, I attached my mityvac to the brake booster nipple on the intake manifold and the vacuum held right at 20". So I'm assuming my intake manifold gasket is good if it will maintain that solid reading. I also did the ECU reprogramming, following the manual precisely.
The good news is that on the third tank of fuel after the grove, the mileage came up. The van, pregroove, on paper was getting 24 mpg and that is also what the digital overhead gauge was reading. Now the gauge is reading 32 on level going. I've noticed the fuel gauge is dropping substantially slower also but I haven't put enough miles on it yet to figure it out on paper. It appears that something positive is happening mpg wise. Appears it just took the ECU some time to reprogram. Thank you for responding to my issue, which it seems may now be a nonissue. I'm open to any suggestions.
I've got a 2014 T & C, 3.6L I've looked at grooving but there are about twice the wires and plugs and cables on that one vs the 05. I'm a little intimidated to start that project. Has anyone done one of those with decent results ? Anything to pay particular attention to ? Thanks