Here is a '03 Ford Focus 2.0 ZX3 TB, in plastic. It got a large Groove, and I filled the huge IAC bypass port w/ JB Weld. Then I drilled a 1/4" dia. hole thru the JB filler to provide air to the IAC. This engine has the Idle Air Control valve downstream on the intake man. across the big IAC duct.
The TB was cleaned, then I used a small file to scratch the plastic surfaces in the IAC port, to give better adhesion to the JB. I cut some card stock from the JB package, covered it in clear box tape then taped the card over the top entrance of the port. I mixed several batches of JB Weld and carefully placed it in the port working from the downstream side. After a 24 hour cure, I removed the card, and smoothed down the JB filler, to give a close match to the contour of the TB entrance walls.
Ford put this huge IAC bypass port and a big radius tapered reduction in the TB bore leading to the throttle entrance/ plate. By filling, smoothing and drilling the 1/4" hole in the filler epoxy, I'm giving a better entry transition to the throttle bore. There should be much less turbulence in the total airflow, and possibly more CFM total potential. This TB has the biggest IAC port I've seen yet- and it's massive in proportion to the throttle bore size. I still wonder why the OEM's put such big IAC bypass ports in so many TB's, maybe they want to ensure the thing can idle even if the TB is completely grunged-up?
Anyway based on experience and Ron's whiteboard explanations, I believe this 1/4" dia hole can give enough air to allow a good idle, even for fast idle at cold start. I also smoothed the top edge of the TB entrance and did a slight radius to the edge of the taper leading to the actual throttle bore w/ sandpaper.
This Groove isn't the prettiest, it got sorta rough towards the right side. I back filled the bore outer wall w/ epoxy, expecting break-thru. It did break through, and in 2 spots I had to add more epoxy to cover tiny holes. And the IAC port was another area needing back-fill, necessitating filling in that yawning port! I'm happy I got full depth w/ the large bit, and the flat Groove floor is pretty good. Obviously Grooving in plastic is far different than aluminum, it goes fast, I turned down Dremel speed a lot.
This TB goes out to our friend Filipp S. in Seattle tomorrow. Filipp has done some homework w/ the Groove, he has already re-gapped the plugs w/ good results. Any results he sends to me I will post in this thread!
Tracy G